Notices
928 Forum 1978-1995
Sponsored by:
Sponsored by: 928 Specialists
View Poll Results: For only a head gasket replacement only on a 16v and no other service work, would you
Pull the motor
67.80%
Leave the motor installed & pull just the heads
32.20%
Voters: 59. You may not vote on this poll

Blown/Damaged Head Gasket?

Thread Tools
 
Search this Thread
 
Old 05-28-2019, 04:08 AM
  #301  
NelaK
Pro
 
NelaK's Avatar
 
Join Date: Apr 2016
Posts: 688
Received 45 Likes on 36 Posts
Default

I vaguely recall this started as a head gasket replacement... At this point you're just shaming anyone else that wants to do a head gasket without redoing the entire engine compartment.
Old 05-28-2019, 08:49 AM
  #302  
Petza914
RL Community Team
Rennlist Member
Thread Starter
 
Petza914's Avatar
 
Join Date: Oct 2007
Location: Clemson, SC
Posts: 25,928
Received 6,525 Likes on 4,157 Posts
Default

Originally Posted by NelaK
I vaguely recall this started as a head gasket replacement... At this point you're just shaming anyone else that wants to do a head gasket without redoing the entire engine compartment.
Yeah, sorry about that. We could rename it the WYAIT thread.
Old 05-29-2019, 04:34 AM
  #303  
Petza914
RL Community Team
Rennlist Member
Thread Starter
 
Petza914's Avatar
 
Join Date: Oct 2007
Location: Clemson, SC
Posts: 25,928
Received 6,525 Likes on 4,157 Posts
Default

Use the Airlift to vacuum fill the cooling system, which went great. Pulled vacuum to 25 on the gauge and had 5 gallons of Dexcool and Distilled water in a 5 gallon bucket with the feed line and it took about 4.5 gallons. I'll top that up after the first drive.


The bigger news is that the Spider intake is installed with the custom silicone couplers marrying the larger diameter Euro legs to the standard intake manifold.

Took me about 6 hours to get to this point. When I test fit the legs to the body, because I had raised the body to clear the knock sensor, I was about 12mm off on the leg ends meeting up to the body ports

I took most of the fueling loose again, changed the way the knock sensor was installed, which let me lower the fueling setup by about 8mm using some shorter vibration dampening mounts that arrived today.

Next I measured the large coupler that joins the spider body to the throttle body and realized there was some space to be gained in that coupler leaving only about 1mm of clearance between the 2 metal flanges that meet in the coupler vs the 4mm or so designed into the OEM one. So, out came the Redback Cutter again and a scrap of 3" silicone hose from my intake projects and I cut a perfectly straight shorter coupler which got me to 11mm of the 12mm I needed. Figured that was close enough but forgot to factor in the about 1mm for the gaskets - perfect.

Here's a shot of the old coupler and from the oil ring inside, you can see the gap that existed between the two flanges. Then a picture of the new silicone coupler installed.






Of course putting it back in I pinched the hard line for the boost gauge so had to loosen the mounting bolts a bit to free and reroute that, but I got it worked out.



Tomorrow (today actually), I'll connect fuel lines, plug wires, the intercooler hoses, the battery, and maybe turn the key to see what happens.
Old 05-29-2019, 09:45 AM
  #304  
j.kenzie@sbcglobal.net
Rennlist Member
 
j.kenzie@sbcglobal.net's Avatar
 
Join Date: Jun 2005
Location: Park Ridge, IL (near Chicago)
Posts: 3,256
Received 48 Likes on 41 Posts
Default

Looks great, Pete. I'm kind of jealous.

Dave
Old 05-29-2019, 09:55 AM
  #305  
Petza914
RL Community Team
Rennlist Member
Thread Starter
 
Petza914's Avatar
 
Join Date: Oct 2007
Location: Clemson, SC
Posts: 25,928
Received 6,525 Likes on 4,157 Posts
Default

Originally Posted by j.kenzie@sbcglobal.net
Looks great, Pete. I'm kind of jealous.

Dave
Thanks Dave. No need to be jealous. You could do it in a couple months too - just have to decide your new bedtime is somewhere between 2-3 AM
Old 05-29-2019, 10:11 AM
  #306  
Chris Lockhart
Rennlist Member
 
Chris Lockhart's Avatar
 
Join Date: May 2001
Location: Taylors, S.C.
Posts: 2,150
Received 10 Likes on 7 Posts
Default

I am truly in awe of how much you've accomplished in such a short period of time. Absolutely amazing.
Old 05-29-2019, 10:18 AM
  #307  
j.kenzie@sbcglobal.net
Rennlist Member
 
j.kenzie@sbcglobal.net's Avatar
 
Join Date: Jun 2005
Location: Park Ridge, IL (near Chicago)
Posts: 3,256
Received 48 Likes on 41 Posts
Default

Originally Posted by Petza914
Thanks Dave. No need to be jealous. You could do it in a couple months too - just have to decide your new bedtime is somewhere between 2-3 AM
You're right, Pete.
It's amazing how well we work, when a project grabs us. I've been there too. My wife thinks I'm crazy during those periods.
Thanks,
Dave
Old 05-30-2019, 02:39 AM
  #308  
Petza914
RL Community Team
Rennlist Member
Thread Starter
 
Petza914's Avatar
 
Join Date: Oct 2007
Location: Clemson, SC
Posts: 25,928
Received 6,525 Likes on 4,157 Posts
Default

REASSEMBLY IS COMPLETE....

.... except for the hood and cowl cover as I need to wash the underside of the hood from the coolant steam that is all over it from the overheating event.

I reconnected the battery and nothing went pop LOL so that's good news. Cycling the key to the accessory position also turned on the heat exchanger fan and pump, as it should. That also ran the fuel pump and showed me 1 fuel fitting that I forgot to tighten - it was the old line I used from the fuel distributor to the cold start valve at the FD side. Tightened it up, cycled the key again and all dry.

Tomorrow, I'll fire it up and see what works, what doesn't, what leaks, what doesn't, set the timing and if all goes well put a few miles on it so I can top up the fluids, do an oil change to swap the BR40 oil for DT50 and install new spark plugs.



Old 05-30-2019, 03:02 AM
  #309  
Rob Edwards
Archive Gatekeeper
Rennlist Member
 
Rob Edwards's Avatar
 
Join Date: Sep 2002
Location: Irvine, CA
Posts: 17,514
Received 2,719 Likes on 1,319 Posts
Default

That is a metric ton of work, looking good! Fingers crossed for startup tomorrow.
Old 05-30-2019, 10:35 PM
  #310  
j.kenzie@sbcglobal.net
Rennlist Member
 
j.kenzie@sbcglobal.net's Avatar
 
Join Date: Jun 2005
Location: Park Ridge, IL (near Chicago)
Posts: 3,256
Received 48 Likes on 41 Posts
Default

Very nice, Pete. I also put vacuum caps on my silicone hose clamps to save my skin. Your car looks fantastic.
Thanks,
Dave
Old 05-30-2019, 11:37 PM
  #311  
Petza914
RL Community Team
Rennlist Member
Thread Starter
 
Petza914's Avatar
 
Join Date: Oct 2007
Location: Clemson, SC
Posts: 25,928
Received 6,525 Likes on 4,157 Posts
Default

Originally Posted by j.kenzie@sbcglobal.net
Very nice, Pete. I also put vacuum caps on my silicone hose clamps to save my skin. Your car looks fantastic.
Thanks,
Dave
It may look fantastic, but I can't get it running right. AFRs are jumping all over the place. Sometimes it goes totally lean and just dies. Other times it goes totally rich and then dies. Other times it seems like it's running out of fuel. I've tried timing numbers from 20-30 DBTDC. I rebaselined the mixture screw at 9.5 turns from fully CCW. I put the Harmonic Dampener at TDC and popped the distributor cap and it's pointing directly at #1, I and put in new spark plugs. I tried a fuel pump jumper and a different FPR and no joy, and this is all without ever leaving the garage, so don't even know what issues will show up under load and boost.

I didn't do any disassembly of the k-jet system - just moved it over from one car to the other, and realize this motor may have different fueling requirements, but I should have been in the ballpark.

It turns over much longer than the other engine used to before firing up and it doesn't run very smoothly once it does, then it fixes itself and the AFR becomes 12-13 and stays there a bit, then starts walking in one direction or the other until it dies.

So, we'll be taking the 911 to SITM in the morning but I'm also not really sure how I'm going to resolve this prior to the Rendezvous. Thinking about trying to sweet talk Carl into heading for Atlanta a couple days early to swing by and work his magic as the other motor he set up was superb - fast start, rock stead idle, good AFR numbers, etc.
Old 05-31-2019, 10:12 AM
  #312  
SwayBar
Rennlist Member
 
SwayBar's Avatar
 
Join Date: Feb 2006
Location: Chicago Bears
Posts: 3,531
Received 325 Likes on 224 Posts
Default

To simplify, I would disconnect the intercooler feed to the engine intake in order to work-on and get the engine to run correctly NA first.

Once that's accomplished, hook-up the supercharger feed to the engine intake.
Old 05-31-2019, 10:39 AM
  #313  
Carl Fausett
Developer
 
Carl Fausett's Avatar
 
Join Date: Dec 2001
Location: Horicon, WI
Posts: 7,005
Likes: 0
Received 60 Likes on 44 Posts
Default

To simplify, I would disconnect the intercooler feed to the engine intake in order to work-on and get the engine to run correctly NA first.

Once that's accomplished, hook-up the supercharger feed to the engine intake.
This is good advice. Disconnect the supercharger (you can leave it mounted, just remove the belt) Start with it being naturally aspirated and get it running right before boosting it. The supercharger masks tuning problems and can make troubleshooting difficult. When running right, hook it back up.

It may look fantastic, but I can't get it running right. AFRs are jumping all over the place. Sometimes it goes totally lean and just dies. Other times it goes totally rich and then dies. Other times it seems like it's running out of fuel. I've tried timing numbers from 20-30 DBTDC. I rebaselined the mixture screw at 9.5 turns from fully CCW. I put the Harmonic Dampener at TDC and popped the distributor cap and it's pointing directly at #1, I and put in new spark plugs. I tried a fuel pump jumper and a different FPR and no joy, and this is all without ever leaving the garage, so don't even know what issues will show up under load and boost.

I didn't do any disassembly of the k-jet system - just moved it over from one car to the other, and realize this motor may have different fueling requirements, but I should have been in the ballpark.
Sounds like you transferred the fuel distributor from the 4.7 to your motor. Chances are good it has varnish in it from the old gas and being stagnent. Injectors and injector lines are suspect too. Diagnose by swapping in your known-good 4.5L fuel distributor and injectors.

Also: check the WUR if you are using the one from the 4.7 They are mis-named, they are THE control regulator on a K-Jet and critical that it be working right. Again, swap in your known-good one from the 4.5L to see if it reacts better to that.
Old 05-31-2019, 02:56 PM
  #314  
Petza914
RL Community Team
Rennlist Member
Thread Starter
 
Petza914's Avatar
 
Join Date: Oct 2007
Location: Clemson, SC
Posts: 25,928
Received 6,525 Likes on 4,157 Posts
Default

Thanks for the responses. I didn't use any fueling from the 4.7L motor (didn't buy that with it) - it was all the stuff that ran perfectly from my 4.5 so no varnish issues

Fuel injectors and lines are brand new. WUR is the one from my 4.5 and that seems to work, as when the car is cold it fires up and runs the best, then I think the WUR shuts down and the engine starts relying on the other settings which is when it starts misbehaving.

The intercooler does complicate the issue as it makes the mixture screw impossible to reach. If I pull off the intercooler then the supercharger wouldn't be doing anything even with the belt attached. Could it not be tuned this way with the metering assembly just open to atmosphere?
Old 05-31-2019, 03:08 PM
  #315  
BC
Rennlist Member
 
BC's Avatar
 
Join Date: Dec 2001
Posts: 25,150
Received 82 Likes on 55 Posts
Default

Maybe try and make the engine run normally first? I always thought the ID of the SS lines was larger, thereby changing the tune requirements.

Things are never as they seem, and CIS is super tricky.


Quick Reply: Blown/Damaged Head Gasket?



All times are GMT -3. The time now is 10:23 AM.