86.5 stock motor: dropped a valve yesterday.
#1
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86.5 stock motor: dropped a valve yesterday.
Just got off the phone with my 40-year experienced European machinest: My valve stem "popped" in half due to fatigue/defects beyond human eye or metallurgy issues.
I had just started up my race car & it had idled for about 30 seconds before I heard a brief clatter (like a tool had slide off the car & was falling through the engine bay), then the engined stopped. I checked the t-belt, was still on, so we tried to re-start in case it WAS a tool that had fallen, but a brief bit of noise while cranking & then it stopped. Then it was seized.
With the breaker bar, engine only turns 45 degrees either way before stopped.
We hoped it was the clutch, but after inspection ascertained it was probably in the rotating assembly or valve train.
A few hours later I had the cams out & saw an odd valve spring retaining assembly on the #4 where the spark plug came out with a mangled ground strap: the valve had snapped just past the retaining assembly: so tip of the valve, both keepers, & the retainer all still together as one assembly. The vavle was no where to be seen: all the way inside the combustion chamber.
I have the head mostly ready to come out tonight so will have ugly, UGLY pictures to share tomorrow.
FWIW, entire engine is stock/resealed 86.5 engine, no track time, head recently R&R'd by me. Machinest said he's seen it before but not very common: he highly doubts it was anything i could have done. I've performed a number of valve jobs before on 928/951 heads & never seen anything like this before. Bummed. I may have to give last rights to my engine tonight.
I had just started up my race car & it had idled for about 30 seconds before I heard a brief clatter (like a tool had slide off the car & was falling through the engine bay), then the engined stopped. I checked the t-belt, was still on, so we tried to re-start in case it WAS a tool that had fallen, but a brief bit of noise while cranking & then it stopped. Then it was seized.
With the breaker bar, engine only turns 45 degrees either way before stopped.
We hoped it was the clutch, but after inspection ascertained it was probably in the rotating assembly or valve train.
A few hours later I had the cams out & saw an odd valve spring retaining assembly on the #4 where the spark plug came out with a mangled ground strap: the valve had snapped just past the retaining assembly: so tip of the valve, both keepers, & the retainer all still together as one assembly. The vavle was no where to be seen: all the way inside the combustion chamber.
I have the head mostly ready to come out tonight so will have ugly, UGLY pictures to share tomorrow.
FWIW, entire engine is stock/resealed 86.5 engine, no track time, head recently R&R'd by me. Machinest said he's seen it before but not very common: he highly doubts it was anything i could have done. I've performed a number of valve jobs before on 928/951 heads & never seen anything like this before. Bummed. I may have to give last rights to my engine tonight.
Last edited by MarkRobinson; 02-29-2012 at 05:00 PM.
#3
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Originals, within spec out of 98k engine. I have extra heads, valves: more concerned about possible damage to the block/rotating assembly and the chance it happening again, though probably pretty remote.
#5
Amazing that this happens in an under .05% case basis after 25 years and 100k miles.
Simply amazing.
Simply amazing.
#6
Race Director
it happens....... Sean had a stock 5.0 S4 engine suck an exhaust valve at Thunderhill a while back.....here is a video of someone following behind him....talk about SMOKE
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it happens....... Sean had a stock 5.0 S4 engine suck an exhaust valve at Thunderhill a while back.....here is a video of someone following behind him....talk about SMOKE
http://www.youtube.com/watch?v=H2Y9Doj60W4
http://www.youtube.com/watch?v=H2Y9Doj60W4
#10
Race Director
Seans engine was UGLY.....think crack in the oil pan from where the rod hit it ugly.... There are pics on here somewhere
#11
Dang Mark, sorry to hear about this, was looking forward to seeing it run.
#12
Former Vendor
That sucks. Sorry about your problem.
Mike Simard had this happen to one of the TRW "aftermarket" 968 intake valves. Right at the base of the lower keeper groove.
If you look at these valves closely, under magnification, the keeper grooves are very chattered from being machined, which will allow a stress riser to form.
You should be able to see something that allowed the crack to form in your pieces.
Mike Simard had this happen to one of the TRW "aftermarket" 968 intake valves. Right at the base of the lower keeper groove.
If you look at these valves closely, under magnification, the keeper grooves are very chattered from being machined, which will allow a stress riser to form.
You should be able to see something that allowed the crack to form in your pieces.
#13
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A few ugly pics. Piston & ( won't chance the rod) are trashed, head can be repaired, block is reusable: just have a little scratch/gouge to fix: delighted about that all things considered. :/
Last picture: the 3" merge towards the turbo off the factory (prior-owner-mutilated cat-removal) Y-pipe.
Last picture: the 3" merge towards the turbo off the factory (prior-owner-mutilated cat-removal) Y-pipe.
Last edited by MarkRobinson; 03-09-2012 at 12:35 PM.
#15
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Yes the last keeper grove it appears is where it popped in half. The keepers, retainer, & tip of the valve are still one assembled unit. :/