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1985 928s no compression right bank

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Old 07-26-2010 | 04:49 AM
  #31  
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Oh yea, here is the 85 vs the 87 that went in and v8 out again.
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Old 07-26-2010 | 06:29 AM
  #32  
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Well, you might drop the exhaust and run a magnet down through the pipes looking for a stray washer or nut. Its happened before.
Old 07-26-2010 | 09:13 AM
  #33  
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the tick could also be a part of the flywheel that has been moved IE one of the crank positon pins try moving the lower bell housing a bit
Old 08-07-2010 | 02:40 AM
  #34  
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OMG She runs Great, few things here and there to adjust as always but a great close to getting done drive today. Did a few other things along the way that were not so much needed but just wanted to!! thanks for the help.
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Old 08-07-2010 | 03:25 AM
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Didn't something look a bit off when the 2mm wider (as well as longer) 87 valves were dropped in?

Anyway, glad it's back to normal. Nice cosmetics too!




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