Pressure Testing Intake/Turbo/I/C
#61
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From: Bangkok, Thailand, Milpitas, CA & Weeki Wachee, FL
I had a very hard time getting all of the crap out of my polished intake. I wound up using Easy-off Blue can and it worked great. I should have taken a before pic, but I forgot. Trust me there was 1/8 - 3/16" worth of black soot everywhere. After an hour of sitting I washed it out with high pressure water and then baked it in the oven at 250 for an hour. I also smoothed out the entrance to the intake with a rotary flap wheel. I did not spend a lot of time making this smooth as there is no way to get most of it done. If Shawn's test of my Extrude Honed intake proves positive, I will get this one done too.
#62
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OK, now for the bad news...
Other than personal satisfaction and some bling, this was a total waste of time! Just like I would have bet I had no vacuum leaks; after finding so many leaks especially the huge one at the turbo, I would have bet this was the cause of all my problems, but after my test drive tonight, I had to make myself a strong drink of JD. The car runs and drives exactly as it did prior to starting this fiasco. I can't tell you what a let down this was! Even my vacuum level which was good before at 16-17 in/hg is the same. Therefore, I can't recommend anybody wasting a ton of time chasing down these leaks.
Other than personal satisfaction and some bling, this was a total waste of time! Just like I would have bet I had no vacuum leaks; after finding so many leaks especially the huge one at the turbo, I would have bet this was the cause of all my problems, but after my test drive tonight, I had to make myself a strong drink of JD. The car runs and drives exactly as it did prior to starting this fiasco. I can't tell you what a let down this was! Even my vacuum level which was good before at 16-17 in/hg is the same. Therefore, I can't recommend anybody wasting a ton of time chasing down these leaks.
#63
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Kind of an interesting footnote that I discussed with Eddie on the phone;
While rinsing the inside of the intake with high pressure high flow water, I noticed an unexpected event. After filling with water all of the water came out of runner number 4. A little came out of 3, but not much. # 1 & 2 had zero flow unless I directly pushed in the hose pointed straight at the port. I figured there would be some flow out of 1 & 2. It did not even come up flush with the intake mounting flange, while all the time gushing out of #4, with probably 4-6" of head pressure above the flange like a fountain. I needed an assistant to take a video. It was quite interesting.
Note: I had a fire hose type of nozzle with a rubber surround which actually fit into the opening flush to seal it.
While rinsing the inside of the intake with high pressure high flow water, I noticed an unexpected event. After filling with water all of the water came out of runner number 4. A little came out of 3, but not much. # 1 & 2 had zero flow unless I directly pushed in the hose pointed straight at the port. I figured there would be some flow out of 1 & 2. It did not even come up flush with the intake mounting flange, while all the time gushing out of #4, with probably 4-6" of head pressure above the flange like a fountain. I needed an assistant to take a video. It was quite interesting.
Note: I had a fire hose type of nozzle with a rubber surround which actually fit into the opening flush to seal it.
#64
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OK, now for the bad news...
Other than personal satisfaction and some bling, this was a total waste of time! Just like I would have bet I had no vacuum leaks; after finding so many leaks especially the huge one at the turbo, I would have bet this was the cause of all my problems, but after my test drive tonight, I had to make myself a strong drink of JD. The car runs and drives exactly as it did prior to starting this fiasco. I can't tell you what a let down this was! Even my vacuum level which was good before at 16-17 in/hg is the same. Therefore, I can't recommend anybody wasting a ton of time chasing down these leaks.
Other than personal satisfaction and some bling, this was a total waste of time! Just like I would have bet I had no vacuum leaks; after finding so many leaks especially the huge one at the turbo, I would have bet this was the cause of all my problems, but after my test drive tonight, I had to make myself a strong drink of JD. The car runs and drives exactly as it did prior to starting this fiasco. I can't tell you what a let down this was! Even my vacuum level which was good before at 16-17 in/hg is the same. Therefore, I can't recommend anybody wasting a ton of time chasing down these leaks.
Sorry bud ..
Back to the drawing board !
Oh BTW that picture on the right looks like my last Colonoscopy
#66
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Yes, a big let down Eddie. Oh well, keep on chipping away at it. Sooner or later this thing will run properly. I really like the gray color vacuum line though. I have plenty if you want to try.
Tom: I have not received S/W patch yet.
Tom: I have not received S/W patch yet.
#67
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When do u think you may get that SW patch ?
Regards
Ed
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Soon, I will let you know. I can bring the tester, line and T's over. We threw a ton of this line/hose away, now I wish I kept more of it. It is really high quality stuff. The color is nice as well, not too flashy.
#69
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#71
Kind of an interesting footnote that I discussed with Eddie on the phone;
While rinsing the inside of the intake with high pressure high flow water, I noticed an unexpected event. After filling with water all of the water came out of runner number 4. A little came out of 3, but not much. # 1 & 2 had zero flow unless I directly pushed in the hose pointed straight at the port. I figured there would be some flow out of 1 & 2. It did not even come up flush with the intake mounting flange, while all the time gushing out of #4, with probably 4-6" of head pressure above the flange like a fountain. I needed an assistant to take a video. It was quite interesting.
Note: I had a fire hose type of nozzle with a rubber surround which actually fit into the opening flush to seal it.
While rinsing the inside of the intake with high pressure high flow water, I noticed an unexpected event. After filling with water all of the water came out of runner number 4. A little came out of 3, but not much. # 1 & 2 had zero flow unless I directly pushed in the hose pointed straight at the port. I figured there would be some flow out of 1 & 2. It did not even come up flush with the intake mounting flange, while all the time gushing out of #4, with probably 4-6" of head pressure above the flange like a fountain. I needed an assistant to take a video. It was quite interesting.
Note: I had a fire hose type of nozzle with a rubber surround which actually fit into the opening flush to seal it.
What is your car doing?
#72
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Thanks Harry, I actually knew this, but the visualization of the water shooting out of only one runner was intriguing to say the least, made me sit back and say Hmmm..., I wonder if we are getting even cylinder filling with this design?
My problem is unfortunately unrelated and don't really want to go into it here. I am working on it with great support from Josh, Shawn, and Tom. We will knock it out soon! I am a bit of a perfectionist, which is not helping things.
I learned a lot about assuming this weekend and was humbled by this simple $10 pressure tester. Can't believe I waited this long to use one.
My problem is unfortunately unrelated and don't really want to go into it here. I am working on it with great support from Josh, Shawn, and Tom. We will knock it out soon! I am a bit of a perfectionist, which is not helping things.
I learned a lot about assuming this weekend and was humbled by this simple $10 pressure tester. Can't believe I waited this long to use one.
#73
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From: Bangkok, Thailand, Milpitas, CA & Weeki Wachee, FL
Just in case anybody wanted to copy my pressure tester design, here is a picture. This design worked out very well.
Last edited by URG8RB8; 10-17-2013 at 11:47 PM. Reason: Reduced Picture Size
#74
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I would have thought you would just use the one on the compressor
but I think your design allows a lot more control
Nice !!!
Regards
Ed
Edit I see its just a gauge not a regulator ;-)
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From: Bangkok, Thailand, Milpitas, CA & Weeki Wachee, FL
Yes, just a shut off valve and gauge so you can do a leak back/down test. Good thing we have this stuff laying around at work, especially for you. If you wanted to buy all those SS Swagelok parts it would cost a pretty penny!