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Why am I getting too much boost?

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Old 03-22-2007, 09:07 AM
  #16  
Geneqco
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Any idea what actually caused it? Sounds like it was almost new?

I was looking at buying a car on ebay that had the same thing happen shortly after install. There was uncertainty as to precisely what damage it had caused - possibly just head gasket. I was prepared to take a chance to a point, but in the end it went for too much.
Old 03-22-2007, 10:51 AM
  #17  
hp18racer
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I have had boost control problems on 3 different occasions on my car. I use a black **** controller and a dual port gate. When it quits, I go through the following:

Set my air compressor to 20psi and pressurized the line that runs to the black **** and waste gate.

If ANY leaks are heard, you can fairly quickly trace them down and find them.

If no leaks then a click should be heard from the waste gate as the valve moves.

If you get no click from the waste gate then take out the black **** and test it on the bench with your 20psi air. You should be able to turn the valve so that it all passes through or so that no air passes through.

If there are no leaks, no black **** problem, and you hear the click but it STILL doesn't work, then take the waste gate out and do the same pressure test on the bench. Blow in the exhaust inlet to the waste gate when you pressurize the control input.
Old 03-22-2007, 11:13 AM
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reno808
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What kind of boost controller your have?
Old 03-22-2007, 11:35 AM
  #19  
hot-J
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black ****........ hp18racer.... very good suggestions, I'll do that now. ST, no blowing in the pipe over here buddy, I personally like bieng the one blown...... God, did that sound like a propositon?
Old 03-22-2007, 11:41 AM
  #20  
ausgeflippt951
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...well you do have a picture of some woman's terrific rear w/ a P tattoo...doesn't seem too far off the mark.

Jesus what am I saying??? No worries, I just woke up...sigh.
Old 03-22-2007, 02:20 PM
  #21  
toddk911
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Originally Posted by 9fitty1
Derek, sir.

I blow the pipe daily, Thanks. Works wonders. You should try it sometime, Tool.
He tried but he keeps falling off the couch.....

Old 03-22-2007, 06:14 PM
  #22  
333pg333
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Originally Posted by Geneqco
Any idea what actually caused it? Sounds like it was almost new?

I was looking at buying a car on ebay that had the same thing happen shortly after install. There was uncertainty as to precisely what damage it had caused - possibly just head gasket. I was prepared to take a chance to a point, but in the end it went for too much.
I think at that time I was having boost spikes due to the then boost controller. It worked fine for a week or so afterwards and since then I've been running a Lindsey dpwg with no problems.
Old 03-23-2007, 03:17 PM
  #23  
HansB
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I had the same problem with the **** dialed all the way down - in fact it generated random boost. Only explaination we could com up with is that the tubes to the wastegate acted as a closed air pressure vessel, with a perssure depending on the temperature.

It was easily solved (after a blown HG) by opening the boost controler to the original setting
Old 03-23-2007, 04:12 PM
  #24  
reno808
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The MBC could be broken. Bo that i think of it. I was running into similer problems. I sloved the issue with a EBC.



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