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90 GT Down on power

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Old 05-16-2017, 11:25 PM
  #46  
Mrmerlin
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113mm tween the nubs?
Old 05-16-2017, 11:52 PM
  #47  
worf928
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Cams are off by a half-link. There should be exactly 6 links between the sprocket teeth that are aligned with the marks.

Might even be a full link off.

Edit: yeah, I think a whole link.
Old 05-17-2017, 01:27 AM
  #48  
zekgb
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Definitely a full link off, but we knew that was gonna be the answer.
Old 05-17-2017, 02:13 AM
  #49  
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Always a bit risky trying to infer alignments on wide angle photos not aligned with the axis being judged but it sure looks as though that inlet cam is one tooth retarded.

Hopefully fortune favours the innocent owner and there has been no mechanical interference. I doubt the motor would even have the low compression pressures recorded had there been mechanical contact but I suppose even the slightest kiss will have some degradation.

Looks like it is time to reinstall the cam train and test compression once more. This time with a bit more supervision?
Old 05-17-2017, 08:30 AM
  #50  
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put rags into the oil return wells before you take any parts off
Old 05-17-2017, 03:13 PM
  #51  
Kevin in Atlanta
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Originally Posted by Mrmerlin
113mm tween the nubs?
106 Yikes!



I've done a few of these and I've never missed.
Old 05-18-2017, 03:07 PM
  #52  
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Time to change those chain runners
Old 05-18-2017, 08:34 PM
  #53  
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Originally Posted by Kevin in Atlanta
These numbers were recorded with the engine cold. Owner performed the test twice after increasing the number of revolutions(7-9).
1 -8 below.
105
115
108
80
190
160
190
178

Car history at the shop in Orlando. Customer (not current owner) has shop do timing belt and water pump. While on test drive tech noticed heavy white smoke. Determines that car needs a head gasket. One cylinder (7) had coolant in it. They pulled the engine and emptied the PO's wallet.

Leak down test is next.

I am still hoping this is poor cam alignment.
No need for a leak down. As speculated the cams are misaligned.

Also, the cylinder psi of each bank are consistent, thus, once properly timed, the motor will be good to go. Although I'd recheck the 80 psi cylinder.
Old 06-07-2017, 01:23 PM
  #54  
Kevin in Atlanta
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Default An update

While the PS was 6 links - nub to nub... the DS was eight. Yikes! Should be back together soon and will get a compression test. Owner is doing all his own work and doing quite well at it.
Old 06-07-2017, 02:38 PM
  #55  
Chris Lockhart
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Originally Posted by Kevin in Atlanta
While the PS was 6 links - nub to nub... the DS was eight. Yikes! Should be back together soon and will get a compression test. Owner is doing all his own work and doing quite well at it.
WOW!! Do we know what shop to stay away from in Fla?
Old 06-07-2017, 03:54 PM
  #56  
Kevin in Atlanta
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But, Chris they averaged to seven. Isn't that ok?
Old 06-07-2017, 04:47 PM
  #57  
Chris Lockhart
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Originally Posted by Kevin in Atlanta
But, Chris they averaged to seven. Isn't that ok?
LMAO!!!!



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