Notices
928 Forum 1978-1995
Sponsored by:
Sponsored by: 928 Specialists

trying to solve slight engine bucking...ideas?

Thread Tools
 
Search this Thread
 
Old 02-21-2016, 11:15 PM
  #121  
GregBBRD
Rennlist
Basic Site Sponsor
 
GregBBRD's Avatar
 
Join Date: Feb 2005
Location: Anaheim
Posts: 15,221
Received 2,458 Likes on 1,460 Posts
Default

Originally Posted by granprixweiss928
Just bumping this thread back up. I have NOT solved this.

What I have done is run the car without O2 connected to get around it.
It got me thru the rest of the show season.

This was not solved ad I want to continue trying things to figure this out.

Mark
Keep in mind that not running the O2 sensor allows the engine to run richer than with it hooked up...and you say this helped. However, reading back, increasing the amount of fuel injected by changing the spring on the door did not help (actually made it worse, as I recall).....note this also richens up the mixture.

Tough, for me, to make these two facts equate.

At any rate, from your last post about the intake leak, you have an obvious cam carrier to cylinder head gasket failure. I thought you were going to remove the intake, cam carriers, and heads once the show season was over?

I'd certainly suggest starting with fixing the obvious and hope that you find the running problem when you do this other work.
__________________
greg brown




714 879 9072
GregBBRD@aol.com

Semi-retired, as of Feb 1, 2023.
The days of free technical advice are over.
Free consultations will no longer be available.
Will still be in the shop, isolated and exclusively working on project cars, developmental work and products, engines and transmissions.
Have fun with your 928's people!





Old 02-22-2016, 03:52 PM
  #122  
granprixweiss928
Three Wheelin'
Thread Starter
 
granprixweiss928's Avatar
 
Join Date: Jun 2013
Location: Norcal
Posts: 1,391
Received 26 Likes on 14 Posts
Default

Originally Posted by GregBBRD
Keep in mind that not running the O2 sensor allows the engine to run richer than with it hooked up...and you say this helped. However, reading back, increasing the amount of fuel injected by changing the spring on the door did not help (actually made it worse, as I recall).....note this also richens up the mixture.

Tough, for me, to make these two facts equate.

At any rate, from your last post about the intake leak, you have an obvious cam carrier to cylinder head gasket failure. I thought you were going to remove the intake, cam carriers, and heads once the show season was over?

I'd certainly suggest starting with fixing the obvious and hope that you find the running problem when you do this other work.
Greg

thanks for your response. Yes I agree its been confusing.

with the 02 unplugged and the adjusted spring on a rebuild AFM, I am getting a nice consistent 14.6-14.7 AFR when driving/cruising.

Yes the plan is to pull the engine and do the head gaskets/cam covers- this spring. My fall/winter work schedule does not allow for car work (and Ive been playing with my new-to-me 997).
Old 03-03-2016, 12:45 AM
  #123  
granprixweiss928
Three Wheelin'
Thread Starter
 
granprixweiss928's Avatar
 
Join Date: Jun 2013
Location: Norcal
Posts: 1,391
Received 26 Likes on 14 Posts
Default

Well I think I have this solved.

I took a chance and picked up used ECU for a good price off ebay.

I figured if, if the new ecu nets the same results then I know for sure its not the ecu in the car, and then Id have a spare on the shelf. I had tried another ecu before, and it didnt solve it. I wanted to try another.

The new Ecu is the later version, 04 from and 84, while the original one in the car is an 02.

I put in the new ecu, reconnected the O2 and took it for a nice spirited drive. It felt way better! Acceleration was smoother and it seemed happier at idle as well. exhaust smelled less rich during warm up.

I then put the original Ecu back in and felt the same issues as before.
switched back to the new ecu tonight and drove it again and its way better!
Old 03-03-2016, 07:25 AM
  #124  
The Deputy
Drifting
 
The Deputy's Avatar
 
Join Date: Dec 2014
Location: Michigan
Posts: 2,177
Likes: 0
Received 2 Likes on 2 Posts
Default

Good news...I hope the fix sticks.

Brian.
Old 03-03-2016, 05:37 PM
  #125  
Brian'sIris
Advanced
 
Brian'sIris's Avatar
 
Join Date: Mar 2015
Posts: 65
Likes: 0
Received 0 Likes on 0 Posts
Default

Originally Posted by xzchgh
Yup !.., me too, ongoing problem for quite some time as well, but not always ?
This guy is a Spammer!!

On topic: Glad to hear your problem is fixed! I have a similar problem with my '85 5-speed. Bucking in cold weather and when engine is cold, goes away when accel. pedal is floored. Bucks violently and rapidly at times...must be hard on the drivetrain! Other times just a gentle bucking while cruizing.

Hoping my (ongoing) intake refresh, etc. takes care of it, but will look here for clues if not.

Cheers,
Brian
Old 12-09-2016, 12:59 AM
  #126  
Hercdriver
7th Gear
 
Hercdriver's Avatar
 
Join Date: Apr 2013
Posts: 7
Likes: 0
Received 0 Likes on 0 Posts
Default My bucking only happens when I come to a stop

I am trying to solve the same problem on a 86.5. The bucking only happens when the car comes to a stop. The car runs smooth otherwise and no bucking while on park or neutral. The bucking is more prominent when the engine is cold.

Thanks in advance
Old 12-09-2016, 01:03 AM
  #127  
Speedtoys
Rennlist Member
 
Speedtoys's Avatar
 
Join Date: Sep 2010
Location: Boulder Creek, CA
Posts: 13,582
Received 1,034 Likes on 623 Posts
Default

What maintenance has been done on it that you know of?
Old 12-09-2016, 11:43 PM
  #128  
granprixweiss928
Three Wheelin'
Thread Starter
 
granprixweiss928's Avatar
 
Join Date: Jun 2013
Location: Norcal
Posts: 1,391
Received 26 Likes on 14 Posts
Default

Let me follow up here with my issue.

I just finished a complete engine out drivetrain overhaul this summer....

https://rennlist.com/forums/928-foru...uild-pics.html

and while the rebuild found issues- like heads with excessive worn guides dumping in lots of oil, and creating lots of carbon build up-

Once all back together again the issue is still there. Its been determined that its the way it is- the fuel management system is an early design and analog(?) and 30+ years old. I have settled that its just the way it is.

and- with the O2 unplugged, its still there, but way less so. but then it stinks when its cold and warming up.
Old 12-11-2016, 12:39 PM
  #129  
Hercdriver
7th Gear
 
Hercdriver's Avatar
 
Join Date: Apr 2013
Posts: 7
Likes: 0
Received 0 Likes on 0 Posts
Default

Hello speedtoys,
Maintenance performed:
Sparks plugs/wires
Both coils.
New MAF(re-built)
I just moved from DC and on cold mornings it was more noticeable, now in Florida is not as severe as in DC. I need to change all vaccum lines and the THrottle position switch. I dont know if I have an iddler valve and location, need to do some more troubleshooting, still learning this engine.
Old 12-11-2016, 12:46 PM
  #130  
bureau13
Rennlist Member
 
bureau13's Avatar
 
Join Date: May 2014
Location: South Florida
Posts: 3,478
Received 55 Likes on 42 Posts
Default

I know the Temp II sensor tells the computers what temperature range its in, so that could be related here. I just ordered one because I have some occasional cold running issues, and because it's the original one (I suspect) and could use with a change. There's a test you can run with an ohmeter but in my case, it's intermittent.

For what it's worth, my original "engine bucking under light throttle" problem was injector related. I'm not exactly sure about what you're seeing though, you mentioned it happens as you come to a stop, which is different.
Old 12-11-2016, 01:54 PM
  #131  
Mrmerlin
Team Owner
 
Mrmerlin's Avatar
 
Join Date: May 2004
Location: Philly PA
Posts: 27,905
Received 2,256 Likes on 1,249 Posts
Default

I would suggest to install a new green wire this was discussed on page two,
but I never saw it noted that a new wire was installed. deox100 all connections.

Remove the connector for the computer in the engine bay and put deoxit 100 on the connector,
then plug it together.

Remove both of the ground wires for the injector system from the right cam tower,
and then remove any brackets and clean them all,
then add deoxit 100 to the connections .

Replace the temp 2 sensor connector and put 100 on the temp 2 sealing ring then tighten it up.

Remove the distributor and on the bench verify that the vacuum advance unit works smoothly.

Use a feeler gauge to verify that the fingers have clearance both while advanced and not advanced.
make sure none of the fingers are bent.

Verify that the roll pin that locks the finger plate to the shaft is still in the groove.

Remove the computer connectors inside the car at the pass footwell and put deoxit 100 on them.

Go to the hatch and find the ground bundle in the RR area of the hatch floor or behind the RR quarter liner loosen the bolt then put deox100 on it, tighten bolt.

Remove both battery terminals and 100 them. same for the ground point connection.

Replace the engine ground strap to chassis. (this step might have been done.)

Replace the O2 sensor with a new factory part.

Put 100 on all of the spark plug wire connections and the coil connections.

Test the coil to see if its performing as it should see WSM.

Please answer every step as I have suggested,
NOTE even if you did it last year follow these suggestions,
please report your findings
Old 12-11-2016, 04:02 PM
  #132  
mkriete
Racer
 
mkriete's Avatar
 
Join Date: Oct 2014
Location: Columbia, Missouri
Posts: 402
Likes: 0
Received 0 Likes on 0 Posts
Default

Originally Posted by granprixweiss928
Let me follow up here with my issue.

I just finished a complete engine out drivetrain overhaul this summer....

https://rennlist.com/forums/928-foru...uild-pics.html

and while the rebuild found issues- like heads with excessive worn guides dumping in lots of oil, and creating lots of carbon build up-

Once all back together again the issue is still there. Its been determined that its the way it is- the fuel management system is an early design and analog(?) and 30+ years old. I have settled that its just the way it is.

and- with the O2 unplugged, its still there, but way less so. but then it stinks when its cold and warming up.
Thanks for the update. I've had a bucking issue at high RPM under load and have been watching this thread closely. Sorry you have not completely solved your issue.



Quick Reply: trying to solve slight engine bucking...ideas?



All times are GMT -3. The time now is 07:53 PM.